( Back in November 2010, amid apparent fuel delivery issues, I limped home after this:
http://www.aleromod.com/forums/showt...152#post566152 )
At last a chance to get in some runs
Upgraded injectors, made an attempt at tuning, experimented a little....
But DAMN, it was good to be out there again.
Beech Bend Raceway Park, Bowling Green, KY, 09/17/2011, 72 degrees F.
M&H Racemaster 8.5 x 24.5 slicks, 36 lb. injectors, base fuel pressure set at 44. Full exhaust, air filter bypassed. Gas tank full, to eliminate possibility of fuel canister running dry.
6:21 PM
Car#-----B888
R/T------.166
60'-----1.990
330-----5.585
1/8-----8.570
MPH-----82.93
1000----11.169
1/4-----13.378
MPH-----101.94
Notes: launch not up to paar. Had best-
looking WOT scan I've seen with this car -- no knock retard whatsoever. Injector Duty Cycle (IDC) : 89 %
7:34 PM
Car#-----B888
R/T------.181
60'-----1.997
330-----5.577
1/8-----8.535
MPH-----83.46
1000----11.110
1/4-----13.296
MPH-----102.98
Notes: Lousy launch again. Added + 1.5 degrees of timing, tweeked the MAF tubing. The IAT in the intake manifold was about 10 degrees F. lower than the first run. IDC -- 94%............ Again, absolutely zero Knock Retard.
8:46 PM
Car#-----B888
R/T------ -.026
60'-----2.041
330-----5.641
1/8-----8.606
MPH-----83.25
1000----11.179
1/4-----13.363
MPH-----103.11
Notes: Launching botchalism continues... Added 2 more degrees of timing, but the PC's battery died after the burnout, so could not analyze data.
Had some strange stuff on the cruising scans lately, but made it the 90 miles back home no problem. Except the exhaust seems louder now, may have shook something loose on the launches.